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NTSB Report Blames Clear Air Turbulence for United Airline Flight Injuries

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    Newfoundland Sikorsky Crash: Final


    Pictured: Couger-owned Sikorsky S-61N Helicopter
    Click to view full size photo at Airliners.net
    Contact photographer Phil Earle
    On March 12, 2009, about 0926 ADT, Atlantic Daylight Time, a Sikorsky S-92A helicopter, Canadian registry C-GZCH, operated by Cougar Helicopters, impacted the waters of the North Atlantic about 28 miles east of Cape Spear near St. John’s, Newfoundland. There were two pilots, Pilot Matthew William Thomas Davis, 34, of St. John’s, Newfoundland and Labrador and First Officer Tim Lanouette, 48, of Comox, British Columbia, both of whomdied in the accident, and 16 passengers on board the helicopter. One passenger, Robert Decker, survived with serious injuries, but the other occupants were fatally injured. The helicopter was en route from St. John’s International Airport (CYYT) to an offshore oil platform in the Hibernia oil field. The pilot made a MAYDAY call due to a mechanical difficulty, and was returning to St. John’s at the time of the accident. Visual meteorological conditions prevailed at the time of the accident, and the sea state had 3 – 5 meter swells. An instrument flight rules (IFR) flight plan was filed.

    The NTSB has recommended that any gearbox losing oil pressure should have the capacity to run dry for 30 minutes before failure. In the case of Flight 491, the elapsed time between the warning light and the ditching of the aircraft in the sea was 11 minutes. Two of the three main gearbox mounting studs were broken. When they broke, the helicopter lost oil rapidly and the gears began to overheat.

    On March 23, 2009, Sikorsky released a bulletin that most of the world’s S-92TM helicopter fleet already had complied with the company notice to retrofit the aircraft’s gearbox oil bowl with steel mounting studs.

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    Air New Zealand Plane Returns to Argentina due to Landing Gear Issue

    Air New Zealand flight NZ-31 had to return and make an emergency landing at Ministro Pistarini International Airport, Buenos Aires, Argentina, on February 8.

    The Boeing 777-200, en-route to Auckland, New Zealand, had to return after it could not retract it’s landing gear. The plane had to dump fuel before landing.

    The plane landed safely.

    No one was injured.

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    Royal Jordanian Airlines Flight Diverted due to Medical Emergency

    Royal Jordanian AirlinesRoyal Jordanian Airlines flight RJ 264 had to divert and make an emergency landing at Montreal airport in Canada, on March 16.

    The flight, en-route from Chicago to Amman, was diverted after a 70-year-old Jordanian passenger became sick midair.

    The Boeing 787 landed uneventfully and the sick passenger was immediately transported to hospital.

    The flight resumed later on, with 224 passengers aboard.

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    American Airlines Flight Makes Emergency Landing at JFK Airport

    American Airlines flight AA-20 made an emergency landing at John F. Kennedy International Airport, New York, on December 25th.

    The Boeing 777-300 plane heading from Dallas/Fort Worth International Airport, Texas, to Heathrow Airport, England, was diverted due to an issue with the lavatories.

    The plane landed safely.

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    Spilled Coffee Cancels Flight


    Click to view full size photo at Airliners.net
    Contact photographer Charin de Silva

    What: United Airlines Boeing 777-200, en route from Chicago O’Hare,IL to Frankfurt/Main
    Where: Toronto
    When: Jan 3rd 2011
    Who: 241 passengers
    Why: While en route, the communication and navigation equipment failed, and the flight crew landed at Pearson as a safety measure. According to the FAA, the apparent reason (or a factor as the investigation is continuing) is that the equipment failed after a crew member spilled coffee on it. Additional confusion followed as pilots sent an incorrect code before they sent the “loss of communication” code.

    UA sent a plane to ferry the passengers back to Chicago and another flight.

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    TAAG Angola Airlines Flight Returns to Luanda After Loss of Cabin Pressure

    TAAG Angola Airlines flight DT-453 had to return and make an emergency landing in Luanda, Angola, on November 11th.

    The Boeing 737-700 plane took off for Namibe, Angola, but had to turn back due to the loss of cabin pressure.

    The plane landed safely. Four passengers were injured; two of them were treated at the airport while the other two were taken to a hospital.

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