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Crew Injured in Turbulent Approach to Oakland

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    Hot Boeing Returns to Mumbai


    Click to view full size photo at Airliners.net
    Contact photographer Jason Whitebird

    What: British Airways Boeing 747-400 en route from Mumbai to London
    Where: Chhatrapati Shivaji International Airport
    When: Thursday Oct 1 2009
    Who: 207 passengers
    Why: Half an hour after takeoff, the fire alarm went off in the cockpit. The plane immediately returned to the airport, landing an hour after takeoff. Passengers debarked safely.

    The only heat maintenance found was hot brakes.

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    American Airlines Flight Diverts to Yakima


    Click to view full size photo at Airliners.net
    Contact photographer Kevin Koske

    What: American Airlines Boeing 737-800 en route from Seattle to Chicago
    Where: Yakima
    When: Oct 04 2010
    Who: 149 passengers and 6 crew, 1 ill passenger
    Why: When a passenger on the flight became ill, the flight diverted to Yakima, where the passenger was taken to Yakima Valley Memorial Hospital after a safe landing. The landing was uneventful except for brakes overheating.

    After a 7.5 hour delay, passengers were back en route.

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    Aeroflot Flight Makes Emergency Landing in Moscow

    Aeroflot flight SU-22 had to return and make an emergency landing in Moscow, Russia, on March 25th.

    The Boeing 737-800 plane took off for Saint Petersburg, Russia, but had to turn back after the crew failed to retract the landing gear.

    The plane landed back safely. All passengers and crew members remained unharmed.

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    Houston-Bound United Airlines Flight Hits Turbulence; 10 Injured

    United Airlines flight UA-1031 encountered turbulence on the way to Houston, Texas, on June 20th.

    The Boeing 737-800 plane was flying from Panama City, Panama, when it hit turbulence that injured nine passengers and one crew member.

    The plane continued for a safe landing. The injured were taken to hospitals.

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    Japan Transocean Air Plane Returns to Japan after Cracked Windshield

    Japan Transocean Air flight NU-44 had to return and make an emergency landing at Naha Airport, Okinawa, Japan, on May 6th.

    The Boeing 737-400 flying to Nagoya, Japan, had to return after the first officer’s windshield cracked.

    The plane landed safely.

    All 148 passengers and 5 crew members remained safe.

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    ALOHA AIRLINES Flight 243

    Aloha Airlines
    Photographer: Juerg Schmid

    NTSB Identification: DCA88MA054.
    The docket is stored on NTSB microfiche number 35379.
    Scheduled 14 CFR ALOHA AIRLINES, INC.
    Accident occurred Thursday, April 28, 1988 in MAUI, HI
    Probable Cause Approval Date: 06/25/1990
    Aircraft: BOEING 737-297, registration: N73711
    Injuries: 1 Fatal,7 Serious,57 Minor,30 Uninjured.
    NTSB investigators traveled in support of this investigation and used data obtained from various sources to prepare this aircraft accident report.
    The Safety Board’s full report on this investigation is provided as Aviation Accident Report number AAR-89/03. To obtain a copy of this report, or to view the executive summary online, please see the Web site at http://www.ntsb.gov/publictn/publictn.htm

    FLT 243 EXPERIENCED AN EXPLOSIVE DECOMPRESSION AND STRUCTURAL FAILURE AT FL240 WHILE ENROUTE FROM HILO, HI, TO HONOLULU, HI. APRX 18 FT OF CABIN SKIN AND STRUCTURE AFT OF THE CABIN ENTRANCE DOOR AND ABOVE THE PASSENGER FLOORLINE SEPARATED FROM THE ACFT. ONE FLT ATTENDANT WHO WAS STANDING IN THE AISLE WAS SWEPT OVERBOARD. THE FLT DIVERTED TO MAUI AND A LANDING WAS ACCOMPLISHED. EXAMINATION OF THE ACFT REVEALED DISBONDING AND FATIGUE DAMAGE WHICH LED TO THE FAILURE OF THE LAP JOINT AT S-10L AND THE SEPARATION OF THE FUSELAGE UPPER SKIN BETWEEN STATIONS 360 AND 540. (SEE NTSB/AAR-89/03)

    The National Transportation Safety Board determines the probable cause(s) of this accident to be:

    FUSELAGE,ATTACHMENT..FATIGUE

    The National Transportation Safety Board determines the probable cause(s) of this accident to be:

    FUSELAGE,ATTACHMENT..SEPARATION

    Contributing Factors

    MAINTENANCE,INSPECTION..IMPROPER..COMPANY MAINTENANCE PERSONNEL

    Contributing Factors

    SUPERVISION..INADEQUATE..COMPANY/OPERATOR MANAGEMENT

    Contributing Factors

    INADEQUATE SURVEILLANCE OF OPERATION..FAA(ORGANIZATION)

    Contributing Factors

    ACFT/EQUIP,INADEQUATE AIRFRAME..MANUFACTURER

    Pdf of official report http://bit.ly/16kpbVy

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