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Lufthansa Airbus Struck by Lightning

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    Door Switch Oops Rolls Nippon Flight


    Click to view full size photo at Airliners.net
    Contact photographer Andrew Bowden

    What: All Nippon Airways Boeing 737-700 en route from Okinawa to Tokyo Haneda
    Where: Hamamatsu
    When: Sep 6th 2011
    Who: 2 crew injured
    Why: While en route, the co-pilot accidentally activated the rudder trim switch instead of the door mechanism.

    The plane descended 6000 feet and rolled, injuring a couple of flight attendants. The first officer—2400 hours— leveled off, and was able to admit the captain who was stuck outside the cockpit, waiting to get in.

    The flight continued without incident.

    In George’s Point of View

    If there is a problem, it comes out, eventually. My pilots tell me that after there is some kind of incident, we need to keep an eye on new incidents, reports, recalls, and especially advisories, directives and safety alerts. There can always be a relationship, no matter how obscure it seems at first glance.

    You know how everyone has been looking at Air France Flight 447 with a new eye, ever since examination into the Air France Flight 471 on July 22 apparently fooled the autopilot into quitting with a swift descent. And Airbus investigators looked at this event twice because you have two the same plane types doing something similar?

    Well, on the surface, this Nippon incident reminds me of Ethiopia Flight 409. It only reminds me because I saw a line drawing of the route of the plane as it spiraled out of control. It also was a 737.

    I’m not calling the situation identical. Certainly if one of the pilots were locked out on a bathroom break—not that a pilot would do this on takeoff!—it would turn up on the voice recorder.

    What if on Ethiopia Flight 409, someone had needed admission into the cabin?

    It just makes me wonder if it is possible that the cabin crew accidentally activated the rudder trim switch. The Ethiopian Airlines plane had just taken off; it would not have been high enough to drop 6000 feet before recovery.

    I know this thought is right out of the blue, and probably has no basis in anything but my wild imagination, but I am told by my pilots that although the switches are dissimilar, the door unlock switch is right next to the rudder trim. So, is it possible the trim switch could have been inappropriately engaged by accident on Flight 409?

    Some airlines rectify this by requiring a third party to open the door if someone leaves the cockpit, but I have to wonder if this could be a design problem.

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    Qantas Encounters Engine-jarring Turbulence over Weipa


    Click to view full size photo at Airliners.net
    Contact photographer Robert Ralph

    What: Qantas/Eastern Australia de Havilland Dash 8-300 en route from Cairns,QL to Weipa,QL
    Where: Weipa
    When: Dec 6th 2011
    Why: On approach to Weipa, the plane flew through a cloud and encountered disruptive turbulence.

    While there were no reports of injury, the turbulence resulted in engine problems. The plane made a safe landing but the incident is under ATSB scrutiny.

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    American Airlines Lands over Fuel Pump Issues


    Click to view full size photo at Airliners.net
    Contact photographer Brian Casity

    What: American Airlines McDonnell Douglas MD-83 en route from Dallas Ft. Worth,TX to Pittsburgh,PA
    Where: near Dallas
    When: Nov 19th 2011
    Why: Just after take-off, the pilot switched the fuel supply from center fuel tank to main wing tanks and the right engine flamed out.

    Pilots returned to the airport and made a safe landing.

    Maintenance is investigating why operating pumps were working, yet failing to provide fuel to the right engine.

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    Condor Sticky Aileron Slows Flight


    Click to view full size photo at Airliners.net
    Contact photographer Giovanni Verbeeck

    What: Condor Boeing 767-300 en route from San Jose Costa Rica to Santo Domingo Dominican Republic to Frankfurt
    Where: San Jose
    When: Jan 11th 2010
    Who: not available
    Why: After takeoff, the Condor Boeing’s left inboard aileron got stuck in the up position. The crew continued at low speed to Santo Domingo where the plane made a safe landing. A replacement jet was provided to complete the route to Frankfurt.

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    Cobham Aviation Plane Returns to Perth due to Engine Issue

    Cobham Aviation flight NC-1990 had to return and make an emergency landing in Perth, Australia, on November 6th.

    The plane took off for Barrow Island, Australia, but had to turn back after the crew needed to shut down one of the engines.

    The plane landed safely. Everyone aboard remained safe.

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    British Airways Flight Makes Emergency Landing due to Engine Issue

    British Airways flight BA-118 made an emergency landing in Munich, Germany, on April 12th.

    The Boeing 777-200 plane heading from Bangalore, India, to Heathrow Airport, England, was diverted due to an engine issue.

    The plane landed safely. All passengers and crew members remained unharmed.

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