George Hatcher's Air Flight Disaster

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George Hatcher's Air Flight Disaster

Turbulence Over Miami

What: American Airlines Boeing 757 en route from Aruba to Miami
Where: Miami
When: July 10, 2012
Who: 185 passengers, 6 crew, 12 injured
Why: While en route thirty minutes from landing, the flight encountered some turbulence. Fifteen seconds worth of turbulence was enough to knock people around. People were knocked out of their seats, and at least one person hit the ceiling. Some of the injured were treated at the airport and some at a Miami hospital.

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Delta Diverts to Cedar Rapids with Engine Trouble


What: Delta en route from Minneapolis to St Louis
Where: Eastern Iowa Airport
When: July 11, 2012, 6 pm
Who: 150 aboard
Why: The Delta flight was en route from Minneapolis to St Louis when it lost an engine. Pilots diverted to Cedar Rapids Iowa and made a safe landing.

Johnson and Linn County fire crews were reported as first responders. No injuries were reported.

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US Airways Charlotte-Rome Diverts for Fumes


Click to view full size photo at Airliners.net
Contact photographer Robert Noël

What: US Airways Airbus A330-300 en route from Charlotte to Rome
Where: Philadelphia
When: July 10, 2012, 10:00 pm
Who: 176 passengers, 12 crew, 5 crew ill
Why: While en route, a number of US Airways flight crew became sick from smelling an odor. The pilot diverted to Philadelphia where they made a safe landing. Passengers were provided an alternative flight.

The flight crew was hospitalized. The fumes that made them ill have not been identified.

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The BEA releases the “Final report” on Air France Flight 447


The BEA report (pp 200-201) concluded:

  • The crew possessed the licenses and ratings required to undertake the flight.
  • The aeroplane possessed a valid Certificate of Airworthiness, and had been
    maintained in accordance with the regulations.
  • The aeroplane’s weight and balance were within operational limits.
  • The aeroplane had taken off from Rio de Janeiro without any known technical
    problems, except on one of the three radio management panels.
  • The composition of the crew was in accordance with the operator’s procedures.
  • The meteorological situation was not exceptional for the month of June in the
    inter-tropical convergence zone.
  • There were powerful cumulonimbus clusters on the route of AF 447. Some of
    them could have been the centre of some notable turbulence.
  • An additional meteorological analysis showed the presence of strong
    condensation towards AF 447’s flight level, probably associated with convection
    phenomena.
  • The precise composition of the cloud masses above 30,000 feet is little known,
    in particular with regard to the super-cooled water/ice crystal divide, especially
    with regard to the size of the latter.
  • Several aeroplanes that were flying before and after AF 447, at about the same
    altitude, altered their routes in order to avoid cloud masses.
  • The crew had identified some returns on the weather radar and made a heading
    change of 12° to the left of their route.
  • At the time of the autopilot disconnection, the Captain was taking a rest.
  • The departure of the Captain was done without leaving any specific instructions
    for crossing the ITCZ.
  • There was an implicit designation of a pilot as relief Captain.
  • There was an inconsistency between the speeds measured, likely following the
    blockage of the Pitot probes by ice crystals.
  • The AP then the A/THR disconnected while the aeroplane was flying at the upper
    limit of a slightly turbulent cloud layer.
  • The aeroplane systems detected an inconsistency in the measured airspeeds. The
    flight control law was reconfigured to alternate 2B.
  • No failure message on the ECAM clearly indicates the detection by the system of
    an inconsistency in measured airspeeds.
  • The pilots detected an anomaly through the autopilot disconnection warning
    that surprised them.
  • The engines functioned normally and always responded to the crew’s inputs.
  • The PNF called out imprecise flight path corrections. They were however essential
    and sufficient for short-term management of the situation.
  • The last recorded values were a pitch attitude of 16.2 degrees nose-up, roll of
    5.3#degrees to the left and a vertical speed of -10,912 ft/min.
  • The Pitot probes installed on F-GZCP met requirements that were stricter than
    the certification standards.
  • Analysis of the events related to the loss of airspeed indications had led Airbus
    and Air France to replace C16195AA Pitot probes by the C16195BA model. The
    first aeroplane had been modified on 30 May#2009.
  • EASA had analyzed Pitot probe icing events; it had confirmed the severity of the
    failure and had decided not to make the probe change mandatory.
  • The flight was not transferred between the Brazilian and Senegalese control
    centres.
  • Between 8 h 22 and 9 h 09, the first emergency alert messages were sent by the
    Madrid and Brest control centres.
  • The crew was not able to use the ADS-C and CPDLC functions with DAKAR Oceanic.
    If the connection had been established, the loss of altitude would have generated
    an alert on the controller’s screen.
  • The first floating aeroplane parts were found 5 days after the accident.
  • The flight recorders were recovered 23 months after the accident.

The accident occurred after the following events:

  1. Temporary inconsistency between the airspeed measurements, likely following
    the obstruction of the Pitot probes by ice crystals that, in particular, caused the
    autopilot disconnection and the reconfiguration to alternate law;
  2. Inappropriate control inputs that destabilized the flight path;
  3. The lack of any link by the crew between the loss of indicated speeds called out
    and the appropriate procedure;
  4. The late identification by the PNF of the deviation from the flight path and the
    insufficient correction applied by the PF;
  5. The crew not identifying the approach to stall, their lack of immediate response
    and the exit from the flight envelope;
  6. The crew’s failure to diagnose the stall situation and consequently a lack of inputs
    that would have made it possible to recover from it.

Download the complete final report here:

BEA FINAL REPORT on AF 447

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Search Continues for Pilot and Crew Missing in Papua New Guinea


What: Hevilift Bell 206
Where: Mt Hagen in the PNG Southern Highlands.
When: July 6, 2012
Who: 3 aboard
Why: A helicopter is missing in Papua New Guinea. The pilot Russell Aikten recently achieved some fame after rescuing victims of the “Black Saturday” fire, and used to fly the Westpac Surf Life Saving Rescue Helicopter.

The Australian Maritime Safety Authority and Hevilift are deploying teams to search for Captain Aikten, Chief pilot Antony Annan, and engineer Emmett Fynn. They left a mayday call about five minutes after leaving the InterOil Drill Rig site at 3.25pm Friday. They were en route to Creek to re-fuel and flying in an area reported to have low visibility at the time.

After days of searching, nothing has been found. Tuesday searchers will be using a helicopter fitted with a magnetometer, used to detect large mineral deposits. They hope it will pick up metal from the missing aircraft. The Australian Defence Force will be deploying two Blackhawks to assist in the search, in addition to the aero-medical evacuation team, additional observers and a downed aircraft recovery team.

See Video Below

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El Al Tel Aviv Flight Returns to Heathrow on Three Engines


Click to view full size photo at Airliners.net
Contact photographer Studzinski Mikolaj

What: El Al Israel Airlines Boeing 747-400 en route from London to Tel Aviv
Where: London
When: Jul 4 2012
Who: 411 passengers
Why: While en route, pilot Ilan Margalit felt that one of the right side engines was losing power as it reached 26,000 feet. He shut down the affected engine and returned to London where he made a safe landing at Heathrow.

The Israel Times reported that the engine caught fire; however other sources say there was no actual fire. The plane landed safely on three engines. A replacement flight was provided on July 5.

The affected engine was a Pratt & Whitney.

In April of 2007 this plane was damaged when it “taxied over its pushback tractor.” No one was hurt in that incident either.

Flight Tracking of ELY318 on O4-July 2012

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TSA Draws a Zero Tolerance Line in the Sand


A group of air marshals which included one supervisor, went to lunch at a restaurant, and eight of them drank alcohol. Some of the marshals were armed. The incident was reported by an Air Marshal who witnessed the incident. The eight who were drinking were fired. Seven of the agents will have a chance to appeal. Six were suspended for not reporting the drinking.

TSA also fired eight Newark security screeners for allegedly sleeping while on duty.

TSA said:

“TSA holds all of its employees to the highest professional and ethical standards and has zero tolerance for misconduct in the workplace,” said Nico Melendez, an agency spokesman. “TSA’s decision to remove the individuals involved in the misconduct affirms our strong commitment to the highest standards of conduct and accountability.”

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Cockpit Odor Causes emergency Diversion

What: Delta flight en route from Puerto Rico to Atlanta
Where: Palm Beach International Airport.
When: July 8, 2012
Who: 180 passengers
Why: After an odor was detected in the cockpit, pilots diverted to Palm Beach and made a safe emergency landing. 120 passengers were rerouted, and sixty were picked up by a replacement flight.

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Spirit Airlines Emergency Landing in Los Angeles

What: Spirit Airlines Airbus A319 en route from Los Angeles to Fort Lauderdale
Where: Houston
When: July 8, 2012
Who: 100+ passengers
Why: After a disruption aboard the flight, the pilots diverted the Spirit Airlines flight to Houston, where they made a safe landing. Passengers who disembarked had no Spirit Airlines counter because, although flights are soon scheduled to begin landing there, currently there is no Spirit Airlines Customer Service at Houston Intercontinental Airport.

On arrival, the disruptive passenger was handed left in the custody of Houston Law Enforcement.

The disruptive passenger was an elderly blind frenchman in his eighties who had become disoriented and frightened. His son was called by authorities.

Passengers reboarded the flight and departed Houston at 6:42 PM.

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Air India Emergency Landing in Pakistan

What: Air India Airbus A-319 en route from Abu Dhabi to New Delhi
Where: Nawabshah 3:37 a.m.
When: July 9, 2012
Who: 122 passengers and six crew
Why: While en route, the flight developed problems with three hydraulic systems. The crew diverted to Nawabshah Pakistan. According to news reports, “The captain preferred to keep passengers on board.”

Air India is sending a team of eight engineers to Nawabshah to repair the plane and return it.

The shuttle sent to return with the stranded passengers is expected to return by 4 pm.

The DGCA is investigating.

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Dana Air Interim Payments Offered


Click to view full size photo at Airliners.net
Contact photographer Peter Tonna
What: Dana Air McDonnell Douglas MD-83 en route from Abuja to Lagos, Nigeria
Where: Iju neighborhood, Lagos
When: June 3, 2012
Who: 153 passengers
Why: Dana air stated that it is fully aware of the mandatory requirement by the International Civil Aviation Organisation (ICAO) and the Nigerian Civil Aviation Authority (NCAA), for interim benefits to be paid to the families of the victims within 30 days of the accident.

Although 68 families have completed their insurance compensation documentation, only nine families were given $30,000 each, having been the only ones to successfully run the legal gauntlet.

Beneficiaries said the interim payment fell short of their expectations.

Claim forms must be taken to Yomi Oshikoya & Co, for verification. Yomi Oshikoya & Co was appointed by the insurers in Lagos.

Dana Air attempted to distribute cheques as interim compensation to some individuals made homeless by the crash. Dana Air prepared N500, 000 for one of the victims, Mr. Daniel Omowunmi, N100, 000, each to two occupants of the boys’ quarters and N200, 000 each to six families in the block of flats. Full payment of the compensation by the insurance company is pending. The lawyer rejected the checks as inadequate and also not all of the victims were included.

In George’s Point of View

Interim payments, that is good.

It’s Lloyds of London.

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Family Piper Lost in Miss. Storm

What: Rgd. Flt Away LLC Piper PA-32R-300 Cherokee Lance en route from Andrews, N.C. to Oxford, Miss
Where: Mississippi
When: July 8 2012
Who: 3 aboard
Why: James Bartley Jr.; his wife, Terry Bartley; and their youngest daughter, Caroline Bartley died when their plane broke apart in the air over Mississippi. They were flying from a vacation home in North Carolina to the University of Mississippi. There was lightning reported in the vicinity when the plane crashed. The wreckage is described as burned and crumpled and may have fallen from an altitude of 8000 feet.

Rescue teams responded on foot, four-wheelers and horseback.

The debris field was spread over half of a mile n a field near County Road 4111 in New Site, Mississippi; the fuselage was found by a medical helicopter.

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Southwest Airlines: Smoke scented Vegas to San Jose Flight


Click to view full size photo at Airliners.net
Contact photographer Conor Clancy

What: Southwest Airlines Boeing 737 en route from Las Vegas to San Jose
Where: Mineta San Jose International Airport
When: July 3, 2012, 10:30 am
Who: 99 aboard, 3 crew
Why: 25 miles east of the airport, the pilot declared emergency. There was no smoke visible but there was the smell of smoke.

The plane taxied to the gate, where passengers disembarked.

Twenty firefighters remained at the scene in case of escalation, as investigators went through the plane.

In George’s Point of View

I fly Southwest and I know enough about aircraft to say that the planes are wearing out.

They are made to take off and land and not stop, but aging planes need extra maintenance. Most of these planes gotta go in for real hard look.

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Melted Tarmac Traps, Delays DC Flight

What: U.S. Airways en route from Reagan National Airport to CHarleston SC
Where: Washington DC
When: July 6, 2012
Who: 35 passengers, 3 crew
Why: As the jet was on the runway, it sank into the hot tarmac, and got stuck. THe cart could not pull the plane with the tires embedded. Everyone aboard disembarked so the jet could get unstuck. Efforts delayed the flight for three hours.

A passenger reported online that there was a jerking motion going back and forth as if something was stuck and preventing the craft from moving, and then passengers waited 45 minutes on the tarmac fir a bus to the terminal.

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Alouette Crashed in Romania, 4 lost

What: Romanian Air Force AR 316B Alouette III
Where: Buzau, Romania
When: July 5, 2012
Who: 4 aboard
Why: Captain Commander Docuz Mitica who was piloting the Alouette when it went down had over 1700 flight hours; and his copilot Viorel Cojocaru had 650 hours. Topoliceanu Catalin had more than 1,100 flying hours, Student Steven Corope?chi also died in the crash. One of the mechanics aboard might have been taking a flying lesson.

The Air Force School of Boboc lost radio contact with the helicopter at around 12:00 shortly before the helicopter crashed in Buzau County in the area known as Cross Comsoaiei right near the highway E85.

Rescue vehicles including water and foam trucks and ambulances responded but all four aboard died.

A committee of Air Force Staff will be investigating the crash and the findings made public.

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UTAir Crashes on 4th, killing 4 in Lensk


Click to view full size photo at Airliners.net
Contact photographer Senior

What: UTAir Aviation Aérospatiale AS 350 B3 Ecureuil en route from Lensk to Talakan
Where: Lensk, Russia
When: July 4, 2012 18:11
Who: 4 aboard, 4 fatalities
Why: Four people were aboard the UTAir helicopter when it crashed near Lensk Russia, killing the pilot and copilot and two passengers just moments after the pilots lost contact with ATC.

Initial reports said there were only three aboard. The helicopter normally performed a regular shuttle flight.
https://airflightdisaster.com/wp-content/uploads/2012/07/aerorussiautair.jpeg

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Commission of Inquiry to Begin

What: Kenya Police Air Wing Eurocopter AS 350B3e Ecureuil
Where: Ngong Hills, near Nairobi Kenya
When: June 10, 2012
Who: 6 aboard
Update: The Kenyan Commission of Inquiry established to look into the June 10 helicopter crash in the Kibiku Forest in Kenya is set to hold its first formal session on July 16. The container holding the wreckage will be stored at the Kenya Police Air-Wing facility at the Wilson Airport.

The Kenya Police Airwing Unit Commandant Rodgers Mbithi will be appearing as the first witness.

The pilots involved, Captain Nancy Gituanja and Luke Oyugi, underwent pilot training in the Ukraine in April 2009.

According to commission members, the intent of the commission is “…not to apportion blame, but to prevent occurrence.”

Fatalities included Minister of State for Provincial Administration and Internal Security George Saitoti and his permanent secretary Orwa Ojode, pilots Luke Oyugi and Nancy Gituanja and bodyguards Inspector Joshua Tonkei and Sergeant Thomas Murimi.

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NC National Guard Firefighting Plane


What: MAFF 7 C-130
When: July 1, 2012 6:30 p.m. Sunday night
Who: Six aboard, including Lt. Col. Paul Mikeal and Master Sergeant Robert Cannon
Why: The tanker made at least two drops of fire retardant on the White Draw fire before it crashed around 6 p.m, the first SUCH crash in the 40-year history of the MAFFS program, a joint Defense Department and U.S. Forest Service program. MAFFS is the Forest Service’s self-contained aerial firefighting system. It can discharge 3,000 gallons covering an area a quarter of a mile long by 100 feet wide in less than five seconds.

Three firefighters were transported by ambulance to a Rapid City hospital. North Carolina state flag have been lowered to half-staff at all state facilities from sunrise to sunset(Tuesday, July 3) to honor the N.C. National Guard members who died.

Charlotte mayor Anthony Foxx said. “On behalf of the City of Charlotte, I would like to extend my deepest condolences to the families and friends of the Airmen who lost their lives Sunday night in South Dakota, and wish the Airmen who were injured a full and speedy recovery,

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Sedona Breakfast Flight Ends in Tragedy

What: Chopper II LLC Aérospatiale AS 350B Astar en route from from Sedona to Scottsdale.
Where: Sedona AZ
When: June 30, 2012
Who: 4 aboard, 4 fatalities
Why: A Aérospatiale AS 350B Astar, N729DP that was reported overdue on Saturday was found by a private pilot at 8:45 a..m. Sunday crashed into the Verde river south of Camp Verde, Arizona. According to FAA reports, “THE 4 PERSONS ON BOARD WERE FATALLY INJURED.”

The wreckage was consistent with a pilot flying at low speed and low altitude.

The remains were found of the pilot, 70-year-old Raymond Perry of Phoenix, 68-year-old passenger Karen Stinn of Cave Creek and 63-year-old Mike Dunaway and 64-year-old Linda Dunaway of Glendale. They were taken to Yavapai County Medical Examiner’s Office. Perry is the CEO of the Arriba Mexican Grill restaurant chain.

A helicopter mechanic reported that it looked as if the chopper nose-dived and the blades from the chopper and the transmission tore through the main cabin where the pilot and passengers were sitting. Wind may have factored in. The helicopter was found in the Verde river.

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SD: More Firefighting Tragedy Strikes

What: USAF Lockheed C-130H Hercules
Where: Edgemont SD
When: 1 July 2012
Who: 6 aboard, 4 fatalities
Why: A C-130 transport aircraft en route to support firefighting missions crashed in South Dakota. The crew was part of the fight against the White Draw Fire.

The USAF Release said:

PETERSON AIR FORCE BASE, Colo. (AFNS) — At approximately 6 p.m. MDT July 1, a Modular Airborne Fire Fighting System equipped C-130 aircraft supporting firefighting missions crashed in the southwest corner of South Dakota. The aircraft was supporting the efforts against the White Draw Fire.

The cause of the crash is not known and the incident is under investigation. There are no details on the status of the aircrew available at this time.

MAFFS is a joint DoD and U.S. Forest Service program designed to provide additional aerial firefighting resources when commercial and private airtankers are no longer able to meet the needs of the forest service.

MAFFS is a self-contained aerial firefighting system owned by the U.S. Forest Service that can discharge 3,000 gallons of water or fire retardant in less than 5 seconds, covering an area one-quarter of a mile long by 100 feet wide. Once the load is discharged, it can be refilled in less than 12 minutes.

Media outlets made this update:
.CHARLOTTE NC – The crash of a North Carolina-based Air National Guard cargo plane that was fighting wildfires in South Dakota has left at least one crew member dead.The family of Lt. Col. Paul Mikeal of Mooresville confirmed they were notified early Monday that he had died in the C-130 crash on Sunday. The 42-year-old married father of two was a veteran of deployments to Iraq and Afghanistan.Lt. Col. Rose Dunlap of the 145th Airlift Wing in Charlotte says six crew members were aboard.The North Carolina Air National Guard confirmed that lives were lost in the crash. Other crew members who were injured were taken to Rapid City Regional Hospital. Names and conditions have not been released.The plane went down about 6 p.m. in the southwest corner of South Dakota where it had been dropping flame retardant on the White Draw Fire.The cause of the crash is under investigation and all other MAFFS-equipped C-130s have been grounded.

In George’s Point of View


So many heroes.
So many tragic deaths.

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Attempted Hijacking foiled

What: Tianjin Airlines Embraer ERJ-190 en route from Hotan to Urumqi
Where: Hotan
When: Jun 29th 2012
Who: 9 crew, 92 passengers
Why: Right after takeoff, six passengers on the flight announced a hijacking.

Apparently three were in the front of the plane, and three were in the back.

Passengers and Sky Marshals subdued the hijackers.

Two flight police officers were seriously injured. Two attendants and seven passengers were slightly injured. The six who attempted to hijack the flight were taken into police custody when the captain returned to the airport within sixteen minutes of takeoff.

b>In George’s Point of View

What a tragic, yet heroic story.

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Russian Pilots Bail out of Sukhoi Jet

What: Sukhoi Su-27UB (“Flanker-C”) 2nd Air Group, 7000th Airbase, Russian Air Force
Where: Besovets, Prionezhsky district, Karelia Republic, Russia
When: June 28, 2012
Who: 2 aboard, 0 fatalities
Why: Col. E. Oleynik and Major general K. Botashov, ejected from a Sukhoi jet before it went down in Besovets village. The air force suspended Sukhoi flights pending investigation. It is not known if the engine ingested a bird or if a flight control system failed.

The jet had been on a routine weather check and training flight.

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Hunan Airlines Crash Report Released; Captain and 19 Others Blamed

The report of the Henan Airlines crash suggests that Henan Airlines be fiend $795,000 due to safety issues and suggests the chief pilot should have his pilot’s license revoked, be removed from his post and expelled from the Communist Party, and should also face criminal charges.

The report says “says chief pilot Qi Quanjun did not locate the runway before landing.” The jet crashed 2260 feet short of the runway. The pilot crash landed under conditions of poor visibility, then left the plane, failed to evacuate the passengers and rescue the injured. The report names 19 people in all as contributing to the accident. Airline officials and local civil aviation authorities are also cited in the report and may be subject to “disciplinary penalties, be demoted or dismissed.”


Click to view full size photo at Airliners.net
Contact photographer Weimeng

What: Shenzhen Airlines/Kunpeng/Henan Airlines Embraer ERJ-190 en route from Harbin to Yichun China
Where: Yichun China
When: Aug 24th 2010
Who: 91 passengers (including 5 children) and 5 crew; 43 immediate deaths, 3 serious injuries and 50 minor injuries
Why: The plane overran the runway—and departed the runway on landing—at Lindu airport in Yichun city in Heilongjiang province at 10:10 p.m, split on impact, exploded, and burst into flames. 53 people were rescued, three of whom with serious injuries.

An investigation in 2008 revealed 100 pilots employed by Henan Airlines’ parent company had falsified their flying credentials; and about a hundred pilots flying for other airlines were found to have done the same thing.

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PR: FAA Proposal of $206,550 Penalty Against Martinaire Aviation

The Federal Aviation Administration (FAA) is proposing a $206,550 civil penalty against Martinaire Aviation, of Addison, Texas, for violating U.S. Department of Transportation Hazardous Materials Regulations.

The FAA conducted a comprehensive hazardous materials inspection at the company’s headquarters on July 8, 2011. As a result of that inspection, the FAA alleges the airline routinely failed to complete documents properly and comply with the requirements for notifying pilots in command about hazardous materials transported as cargo.

The allegations involve 17 shipments of hazardous materials Martinaire accepted for transportation by air on 12 flights between April 1 and June 22, 2011. Martinaire is a scheduled air cargo and cargo charter company. The flights operated between various cities across the country.

Martinaire has 30 days from the receipt of the FAA’s enforcement letter to respond to the Agency.

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Two Fatalities in Portuguese Cessna Crash on Training Flight

What: Cessna 152
Where: Matarraque, S. Domingos de Rana Portugal
When: June 26, 2012 22:33
Who: 2 fatalities
Why: A pilot of the Leávia flight school and a student pilot had made one pass at the runway at Tires aerodrome in Cascais, and had circled to make another pass when they crashed on a training flight. The plane impacted between residences in Matarraque, Sao Domingos de Rana, Portugal.

Judging by proximity, investigators conjecture that the pilot may have been intending to make an emergency landing on the A5. The plane ended up in a yard between two houses on Saudade street about two miles from the airfield. The plane crashed but did not burn. There were no casualties on the ground. Emergency responders included corporate volunteer firefighters and and an ambulance from the National Institute of Emergency Medicine.

The instructor was 45 and his student was in her twenties.

Witnesses say they heard the engine stop before the plane crashed. The “Gabinete de Prevenção e Investigação de Acidentes com Aeronaves” is investigating.

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