August 6, 2013
WASHINGTON – In its continuing investigation of the July 22 accident in which Southwest Airlines flight 345, a B-737-700, landed hard at New York’s LaGuardia Airport (LGA), the National Transportation Safety Board has developed the following factual information:
• The captain has been with Southwest for almost 13 years and has been a captain for six of those years. The captain has over 12,000 total flight hours, over 7,000 of which are as pilot-in-command. In 737s, the captain has over 7,900 hours, with more than 2,600 as the pilot-in-command.
• The first officer has been with Southwest for about 18 months. The pilot has about 5,200 total flight hours, with 4,000 of those as pilot-in-command. In 737s, the first officer has about 1,100 hours, none of which are as the pilot-in-command.
• This was the first trip the flight crew had flown together and it was the second leg of the trip. The first officer had previous operational experience at LGA, including six flights in 2013. The captain reported having flown into LGA twice, including the accident flight, serving as the pilot monitoring for both flights.
• The en route phase of the flight, which originated in Nashville, was characterized by the flight crew as routine. On approach into LGA, the first officer was the pilot flying and the captain was the pilot monitoring. SWA 345 was cleared for the ILS Runway 04 approach.
• The weather in the New York area caused the accident flight to enter a holding pattern for about 15 minutes. The crew reported that they saw the airport from about 5-10 miles out and that the airplane was on speed, course and glideslope down to about 200-400 feet.
• The crew reported that below 1,000 feet, the tailwind was about 11 knots. They also reported that the wind on the runway was a headwind of about 11 knots.
• SWA 345 proceeded on the approach when at a point below 400 feet, there was an exchange of control of the airplane and the captain became the flying pilot and made the landing.
• The jetliner touched down on the runway nose first followed by the collapse of the nose gear; the airplane was substantially damaged.
At this point in the investigation, no mechanical anomalies or malfunctions have been found. A preliminary examination of the nose gear indicated that it failed due to stress overload.
Investigators have collected five videos showing various aspects of the crash landing. The team will be analyzing these recordings in the coming months.
Parties to the investigation are the Federal Aviation Administration, Boeing Commercial Airplanes, Southwest Airlines, and the Southwest Airlines Pilots Association.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
A simulation has revealed a pilot’s last words before flight AF447 crashed in 2009.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
Southwest plane nearly crossed runway in front of departing JetBlue plane Thursday in Virginia
To include the featured image in your Twitter Card, please tap or click their icon a second time.
Russian military plane crashed in Stavropol region
To include the featured image in your Twitter Card, please tap or click their icon a second time.
KYIV, Ukraine (AP) — Ukraine’s air force claimed Friday it shot down a Russian strategic bomber, but Moscow officials said the plane crashed in a sparsely populated area due to a malfunction after a combat mission. Neither claim could be independently verified. Previous Ukrainian claims of shooting down Russian warplanes during their more than two-year […]
To include the featured image in your Twitter Card, please tap or click their icon a second time.
The former president’s aircraft has been seen parked at LaGuardia Airport in New York as he takes part in his hush money trial in Manhattan.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
A military plane crashed in Russia’s Krasnogvardeysky district of the federal city of St. Petersburg. The pilots, according to sources, were ejected safely., Europe News – Times Now
To include the featured image in your Twitter Card, please tap or click their icon a second time.
Two aircraft nearly crashed into each other earlier Thursday at Washington D.C.’s Reagan National Airport.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
Boeing, with its airplane-making reputation in tatters, has revealed plans to get into the flying car market in Asia.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
Lawmakers said it was a “horrifying example” of the effects of undermining slot and perimeter rules, calling the airport’s runway “overburdened.”
To include the featured image in your Twitter Card, please tap or click their icon a second time.
But he notes a more defensive tone coming from the under-fire aviation manufacturer.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
GREEN LAKE COUNTY, WI (WTAQ-WLUK) – A plane heading to EAA Airventure last July probably crashed because it ra…
To include the featured image in your Twitter Card, please tap or click their icon a second time.
The Bonanza pilot didn’t follow the published traffic pattern, placing the aircraft close to rising terrain on downwind. He was too fast on final approach, and he went around on the first attempt. A police officer arrived to check on the airplane, as the pilot had reported to ATC that he was low on fuel. Still, he was safely on the ground.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
A NASA pilot is ready for the Pittsburgh Steelers to kick off the 2024 season.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
This deep-sea footage shows inside a sunken passenger plane, once thought to be the wreckage of the missing Malaysia Airlines flight MH370. The wreckage of the MH370, which disappeared without trace while en route from Kuala Lumpur to Beijing in March 2014, has still never been found. The wreckage filmed by Deep Blue Dive Center, is actually the Lockheed Martin’s L1011 Tristar plane, which was deliberately sunk in 2019 in Jordan. It serves as a home for sea life, but a viral social media post wrongly speculated it was the MH370, which disappeared in 2014.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
The rarely seen footage comes as the company fiercely fights back following a whistleblower’s testimony on Capitol Hill, where a longtime engineer made some alarming allegations.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
Several months after her viral moment, Tiffany Gomas has garnered fresh attention with an eye-catching new post.
To include the featured image in your Twitter Card, please tap or click their icon a second time.
My wife and I are scheduled for an Alaskan cruise in the fall. By all accounts, it’s something to which we should look forward. I’ve been told the same thing about other trips, including a Vegas…
To include the featured image in your Twitter Card, please tap or click their icon a second time.
In the nearly two decades of A380 operations, the superjumbo has never suffered a fatal accident. Why is this and does that make it the world’s safest aircraft?
To include the featured image in your Twitter Card, please tap or click their icon a second time.
To include the featured image in your Twitter Card, please tap or click their icon a second time.