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Category: <span>audio</span>

Co-pilot accused of hijacking Ethiopian Airlines flight


The Eithiopian Airlines Boeing 757 flown from Addis Ababa to Geneva instead of its intended destination Rome was commandeered by its co-pilot, who was seeking asylum in Geneva.

The co-pilot told ATC the plane was being hijacked, and after he landed, climbed down a rope from the cockpit, and told ground police forces that he was the hijacker.

Ethiopia, which has a reputation of targeting journalists, opposition and minorities, has a deteriorating human rights record, and owns Ethiopia Airlines. Charges against the co-pilot could result in a twenty year prison sentence.

No one was injured in the hijacking, but two Italian fighter jets “escorted” the plane to Geneva. Two hundred and two people were aboard.



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Pilots Ignore ATC Directions, Hear Audio

On March 11, 2013, an Air Canada Embraer ERJ-190 en route from Edmonton to Toronto,ON was on approach when ATC informed the pilots to abort the landing. Ground radar indicated something moving on the runway. Pilots continued to make the landing, and ignored ATC.

Mechanics working on a Sunwing Boeing had left a van running and in gear, which subsequently rolled without a driver across the runway. At some point, the van impacted the Sunwing 737.

In George’s Point of View


While we can’t make assumptions, apparently the pilots saw the van safely flew over it and made a secure landing.

However, there are a lot of errors here that could have been disaster. We are glad no one was injured. Safety first, everyone!

  • The maintenance crew for failing to secure their vehicle.
  • ATC for not using the call sign, even if it was evident to them who they were speaking to.
  • Pilots for ignoring ATC even if they saw the “threat” because there could have been an additional alert

That said, of course we are glad no one was injured.

Click Triangle below to hear audio

[sc_embed_player fileurl=”https://airflightdisaster.com/wp-content/uploads/2013/03/Air-Canada-178-Ignores-Go-Around.mp3″]


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Woman Dies in Venezuela Crash, Survivors Rescued

On Feb 2, 2013, a privately owned Beechcraft 58 Baron with six aboard crashed in the Gulf of Cariaco, Venezuela.

The flight had taken off from Puerto Ordaz Airport and was en route to DelCaribe Gen S Marino Airport but suffered a complete loss of engine power. The pilot declared an emergency due to failures in both engines.

Fishermen found the plane located 15 nautical miles (28 km) east of Cumana in the Gulf of Cariaco.

Two of the passengers were reported to be minors.

There was one fatality, a sixty-two year old woman, Vetide Ramos, who died in the crash. Five survivors were brought ashore in a boat, including Ruben Herrera, Poztty Ramos, Jose Ramos, Ivan Herrera (a minor) and pilot Jhonatan Mata.

Audio Below


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Fed Ex Flight Returns to Philadelphia

What: Fed Ex Boeing 727-200
Where: Philadelphia
When: September 19, 2012 11:05PM
Who: Flight crew
Why: Audio below of the Fed Ex flight as it turns back to Philadelphia as the number one engine loses oil.


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OLT Cabin Pressure, Fire, Emergency Diversion


Click to view full size photo at Airliners.net
Contact photographer Pawel Cieplak

What: OLT Express Airbus A320-200 en route from Warsaw to Hurghada
Where: Sofia
When: May 17, 2012
Who: 147 passengers and 8 crew
Why: While en route, cabin lost pressure. The crew descended to save levels and diverted to Sophia.

On descent, pilots reported a fire in the cabin. A hot oxygen generation unit set carpeting on fire. Fire extinguishers on board were used.

Passengers disembarked without injury via slides.

OLT Express is a new Polish airline whose first official flight was publicly touted as April 1, 2012. OLT was formerly LOT and also YES Airways, and is currently running under the ownership of Amber Gold Group.

Looks like they need to work on their maintenance.

Feed from Live ATC


Pilot’s audio provided by http://www.liveatc.net


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US Airways Punched in the Nose Bird Strike


Click to view full size photo at Airliners.net
Contact photographer Cary Liao

What: US Airways Boeing 757-200 en route from Philadelphia,PA to Orlando,FL
Where: Orlando
When: May 11th 2012
Why: The flight was en route when there was a bird strike impacting the nose. The bird made a “significant” dent in the plane. ATC says “Looks like you guys got punched in the nose, US Air”

Play the pilot’s audio below:


Pilot’s audio provided by http://www.liveatc.net


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United Visual Landing Without Instruments, Boston


Click to view full size photo at Airliners.net
Contact photographer Jason Whitebird

What: United Airlines Airbus A320-200 en route from Chicago to Boston
Where: Logan International
When: Oct 23, 2012
Who: 144 passengers, 5 crew
Why: The pilot was on approach to Logan when he noticed a problem with his instruments.

The pilot informed ATC of instrument failures and pressurization issues. ATC cleared a holding pattern, until the pilot performed a visual landing.

The pilot taxied to the Terminal C gate at 12:42 pm. Below is the pilot’s audio.

Pilot audio

Pilot’s audio provided by http://www.liveatc.net

Incapacitated Pilot Circles Gulf

Updated with audio clip

What: Lee H Aviation Inc. Cessna 421C en route from Slidell, La., to Sarasota, Fla.
Where: Gulf of Mexico
When: April 19 2012
Who: pilot
Why: The plane took off normally from Slidell at 6:43 a.m., but en route lost contact with ATC and began flying in circles over the Gulf of Mexico.

Around 8:45 a.m, two F-15s that flew in to check on the plane found it flying between 25,000 and 35,000 feet with the windshield iced over. The pilot remained unresponsive. The plane landed “softly” intact and right side up in the water around 12:10 p.m., approximately 120 miles west of Tampa. The pilot was unconscious or incapacitated.

The 87-foot cutter Coho was scheduled to respond as well as a HC-144 plane from Mobile, Alabama and a MH-60 helicopter in Clearwater.

The pilot may have lost consciousness due to hypoxia, or a lack of oxygen.


Pilot’s audio provided by http://www.liveatc.net


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ALOHA AIRLINES Flight 243

Aloha Airlines
Photographer: Juerg Schmid

NTSB Identification: DCA88MA054.
The docket is stored on NTSB microfiche number 35379.
Scheduled 14 CFR ALOHA AIRLINES, INC.
Accident occurred Thursday, April 28, 1988 in MAUI, HI
Probable Cause Approval Date: 06/25/1990
Aircraft: BOEING 737-297, registration: N73711
Injuries: 1 Fatal,7 Serious,57 Minor,30 Uninjured.
NTSB investigators traveled in support of this investigation and used data obtained from various sources to prepare this aircraft accident report.
The Safety Board’s full report on this investigation is provided as Aviation Accident Report number AAR-89/03. To obtain a copy of this report, or to view the executive summary online, please see the Web site at http://www.ntsb.gov/publictn/publictn.htm

FLT 243 EXPERIENCED AN EXPLOSIVE DECOMPRESSION AND STRUCTURAL FAILURE AT FL240 WHILE ENROUTE FROM HILO, HI, TO HONOLULU, HI. APRX 18 FT OF CABIN SKIN AND STRUCTURE AFT OF THE CABIN ENTRANCE DOOR AND ABOVE THE PASSENGER FLOORLINE SEPARATED FROM THE ACFT. ONE FLT ATTENDANT WHO WAS STANDING IN THE AISLE WAS SWEPT OVERBOARD. THE FLT DIVERTED TO MAUI AND A LANDING WAS ACCOMPLISHED. EXAMINATION OF THE ACFT REVEALED DISBONDING AND FATIGUE DAMAGE WHICH LED TO THE FAILURE OF THE LAP JOINT AT S-10L AND THE SEPARATION OF THE FUSELAGE UPPER SKIN BETWEEN STATIONS 360 AND 540. (SEE NTSB/AAR-89/03)

The National Transportation Safety Board determines the probable cause(s) of this accident to be:

FUSELAGE,ATTACHMENT..FATIGUE

The National Transportation Safety Board determines the probable cause(s) of this accident to be:

FUSELAGE,ATTACHMENT..SEPARATION

Contributing Factors

MAINTENANCE,INSPECTION..IMPROPER..COMPANY MAINTENANCE PERSONNEL

Contributing Factors

SUPERVISION..INADEQUATE..COMPANY/OPERATOR MANAGEMENT

Contributing Factors

INADEQUATE SURVEILLANCE OF OPERATION..FAA(ORGANIZATION)

Contributing Factors

ACFT/EQUIP,INADEQUATE AIRFRAME..MANUFACTURER

Pdf of official report http://bit.ly/16kpbVy

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